Finally got everything in order for another track visit... I hope.
Blew off the throttle body coupler early today. Found the BOV wasn't working, spring was too strong I guess. Dropped in the next lightest spring and it was open at idle.

So I got out the old MAP gas torch and put the original BOV spring in the vice and cranked it down a half inch or so. The hit it with the torch. Lucked out and it seems to work now. I can actually hear it vent and haven't had anymore coupling failures since.
Got a good 10 tuning passes on the street today. I've got it all dialed in at 12 psi & 18* of timing. Feels healthy! I'm guessing 130+ and low 10's with a lazy foot brake launch.